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升流缺氧/好氧脱氮工艺处理生活污水的研究
汪翠萍 ; 魏拓 ; 郑明霞 ; 王凯军 ; WANG Cui-ping ; WEI Tuo ; ZHENG Ming-xia ; WANG Kai-jun
2016-03-30 ; 2016-03-30
关键词A/O工艺 升流缺氧/好氧工艺 城市生活污水 脱氮 anoxic /oxic process up-flow anoxic /oxic process municipal domestic sewage nitrogen removal X703
其他题名Up-flow Anoxic /Oxic Process for Nitrogen Removal in Domestic Sewage Treatment
中文摘要对传统A/O工艺和升流缺氧/好氧(UA/O)脱氮工艺处理城市生活污水的效果进行了对比研究。结果表明,在HRT、SRT、DO、pH值、混合液回流比、污泥回流比、好氧段MLSS等运行参数相同的情况下,A/O和UA/O两组工艺对COD的去除效果相当,平均去除率分别为88%和89%;对NH3-N的去除效果也相差不大,平均去除率分别为90%和92%;但UA/O工艺对TN的去除效果更好,平均去除率为57%,比A/O工艺高了12%。另外,在进水水质波动较大的情况下,UA/O工艺的抗冲击负荷能力更强,出水水质更稳定。; The efficiencies of up-flow anoxic /oxic( UA /O) and conventional A /O process for municipal domestic sewage treatment were studied comparatively. The results showed that under the same operating parameters,such as HRT,SRT,DO,pH,mixed-liquor return ratio,sludge return ratio and oxic MLSS,the A /O process and the UA /O process had similar COD removal efficiencies,and the average COD removal rates were 88% and 89%,respectively. There was not much difference in NH3- N removal efficiency between the two processes,the average NH3- N removal rates were 90% and 92%,respectively. The UA /O process achieved 57% of the average TN removal rate,which was 12% higher than the A /O process. The UA /O process had stronger shock load resistance and more stable effluent quality when fluctuation in influent quality was large.
语种中文 ; 中文
内容类型期刊论文
源URL[http://ir.lib.tsinghua.edu.cn/ir/item.do?handle=123456789/144215]  
专题清华大学
推荐引用方式
GB/T 7714
汪翠萍,魏拓,郑明霞,等. 升流缺氧/好氧脱氮工艺处理生活污水的研究[J],2016, 2016.
APA 汪翠萍.,魏拓.,郑明霞.,王凯军.,WANG Cui-ping.,...&WANG Kai-jun.(2016).升流缺氧/好氧脱氮工艺处理生活污水的研究..
MLA 汪翠萍,et al."升流缺氧/好氧脱氮工艺处理生活污水的研究".(2016).
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